Movements in the blue tube have been tested to see if they work properly. We need to change some connections so it seemed wise to check the current situation before that. Everything works fine. We have also connected the Velocity Selector (VS). It works, but more tests are necessary.
At the moment we are trying to solve a problem with the detector translation stage. It seems to skip some of the built in microswitches and therefore changes its current position along the way. On the next valid switchposition the current position is corrected and the cycle restarts.